Next the elevator pushrod was connected to the control system through to the control column. Although the mechanism worked correctly there was inadequate movement of the elevator - the plans call for 30 degrees up and 25 down. After spending some time pondering this and looking at the options it seemed that moving the control column pivot point forward was the answer. Re-reading the plans made it clear that I didn't have enough horizontal distance between the control pivot point and where the elevator pushrod enters the aileron torque tube. Luckily this wasn't a difficult fix. The pivot hole was re-drilled an inch forward and the original hole plugged with a short piece of 5/16" rod welded into place. The new hole was lined with a piece of 3/8" * 0.028" tube as before. The trim lever rod also had to be lengthened by an inch so a new section was welded in place around a length of 7/16" tube to provide additional strength. Finally the system was re-assembled and I now have 31 degrees up and 25 degrees down - perfect. In addition with the original rework I had done on the system the movement is perfectly smooth, frictionless and without any discernable play - that will do!